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THIS IS A DRILLING REPORTS PAGE FOR THE BSM WILDMAN EAST # 1

See attached Drilling information

Drilling Permit – Wildman

Wildman Spud Date

Proposed Road Access and Surface Location – Wildman

 Water Board Letter – Wildman

DRILLING PROGNOSIS

12-20-18    The test well is expected to spud Saturday or if not, then the day after Christmas.  If Saturday spud, the rig will drill to surface casing depth and set pipe –then will be shut down for Christmas Day.

12-26-18    Bit at 658′ at 3.20 pm Spudded at 7.30 am today.

12/28/2018    This morning, the rig completed running 1604’ of 9 5/8” surface and cemented it to the surface with no lost circulation.  The Texas Railroad requires a heat survey of the pipe to insure that the cement covered the pipe properly to protect the upper ground water.  Drilling ahead will begin usually around six to eight hours after the cement in the surface is complete.

06:00 07:00 1.00 5 TIH 15 JTS OF DRILL PIPE, SEND SWEEP AND CIRCULATE 07:00 09:00 2.00 6 POOH AND BREAK DOWN BHA 09:00 10:00 1.00 1 HAVE PJSM , RIG UP FLOOR AND LOAD RACKS FOR CASING HAD ISSUES GETTING CASING POWER UNIT STARTED HAD TO SWAP TO THERE BACK UP UNIT 10:00 11:30 1.50 12 HAD TROUBLES WITH CASING PWER UNIT, HAD TO SWAP MACHINES AGAIN 11:30 14:00 2.50 12 MADE UP SHOE AND FLOAT, RAN 38 JTS OF 9.5/8 CASING 14:00 18:00 4.00 5 RIG DOWN CASING TOOLS, WORK PIPE WHILE WAITING ON CEMENTERS PUMP TRUCK TO ARRIVE ON LOCATION IT BROKE DOWN IN ROUTE. AT 1400 HR CEMENTER ARRIVED ON LOCATION WITH BULT TRUCKS AND CIR HEAD, PUMP TRUCK BROKE DOWN LEAVING SHOP AT 1500 HR I CALLED PAT WITH BASIC HE SAID HE HAD A TRUCK LEAVING SHOP THEN AT 1930 HR CEMENT HAND CAME IN SAID TRUCK WAS JUST LEAVING HEANDERSON HEADED THIS WAY 18:00 21:30 3.50 12 CIRCULATE AND WORK CASING WHILE WAITING ON CEMENT PUMP TRUCK 21:30 23:00 1.50 12 PUMP TRUCK ARRIVED ON LOCATION @ 2130 / RIG UP CEMENTERS 23:00 00:30 1.50 12 HELD PJSM AND PUMPED 20 BBL SPACER PMP 12.5 PPG LEAD YIELD 2.05, 368 SKS CEMENT/ PMP TAIL 15.6 PPG YIELD 1.18 229 SKS/ BUMPED PLUG AT 0030 / 400- 1000 PSI HELD 5 MIN GOT 1 BBL BACK/ GOT NO RETURN CEMENT BACK TO SURFACE / WE DIDNT LOSE RETURN 00:30 06:00 5.50 21 CALL TRRC SAID NEED TO DO TEMP. LOG / WAIT ON PIONEER WIRELINE

 12-29-18    As you see at the end of this report, the rig is having issues and waiting to be repaired as soon as a service company arrives.

HOUSEKEEPING AND PREVENTITIVE MAINTANENCE WHILE WAITING ON LOG TRUCK 11:00 12:30 1.50 11 RIG UP WIRELINE LOG, RAN TEMPERTURE LOG TO FIND OUT WHERE CEMENT IS SET 430FT. 12:30 18:00 5.50 1 RIG UP 1″ STEEL LINES FOR TOP OUT JOB, WAIT ON CEMENT TRUCK TO RETURN WITH MORE CEMENT 18:00 20:00 2.00 21 WAIT ON CEMENT TRUCK TO ARRIVE TO TOP OFF CASING 20:00 23:30 3.50 12 RIG UP CEMENTERS AND M/U 160 1” PIPE AND TOP OUT PMP 190 SKS CLASS A 2% CACI 15.6LBS. 1.18 YIELD GOT 5 BBLS BACK 23:30 00:00 0.50 12 RIG DOWN CEMENTERS 00:00 03:00 3.00 21 CUT CASING AND WELD ON WELLHEAD 03:00 06:00 3.00 8 HYDRAULIC FEED SYSTEM TO RIG MALFUNTIONING / NOTHING IS OPERABLE TROUBLESHOOTING FOR PROBLEM

12-30-18    It is still experiencing daily issues with the drilling rig.  The only thing we can do at this time is be patient.  The rig will be fixed and drilling will continue.

06:00 18:00 12.00 14 NIPPLE UP STACK, HCR VALVE, BELL NIPPLE, FLOW LINE, GAS BUSTER, CUMMI AND ALL LINES, 3″ FILL UPHOSE, 3″CHOKE LINE,AND TROUBLE SHOOT WINCH INTERFERENCE SENSOR 18:00 03:00 9.00 8 REPAIR RIG / TROUBLE SHOOT WINCH INTERFERANCE SENSOR WITH ELECTRICIAN VIA SCHRAMM TECHNICIAN 03:00 03:30 0.50 21 AIR BLEED AND TRAIN VLV B-02 PV:5 TOP DRIVE TILT 03:30 04:00 0.50 21 M/U AND TORQUE T.I.W. AND BURNSUB TO SPEC AND INSTALL CLAMP 04:00 06:00 2.00 21 P/U AND CLEAN UP TOOLS / GENERAL HOUSEKEEPING WHILE WAITING ON B.O.P. TESTERS

12-31-18    Right now the well is down due to a problem with the top drive.  A welder is called to come and make the repair.  A little over 2500’ has been drilled at this time.  Will update tomorrow and Happy New Year to everyone.

06:00 10:30 4.50 15 TEST B.O.P. , PIPE RAMS, BLIND RAMS, HCR VALVE, LEFT AND RIGHT SIDE OF CHOKE MANIFOLD, @2500 PSI, TESTED SURFACE CASING @1000 PSI 10:30 12:00 1.50 6 TRIP IN HOLE TAG BOTTOM @1539′ 12:00 16:00 4.00 21 DRLG FLOAT EQUIPMENT 16:00 16:30 0.50 2 DRILL FROM 1602 T 1615 AND CIR FOR FIT TEST 16:30 17:00 0.50 21 FIT TEST EQIVALENT TO A 10LB MUD 17:00 17:30 0.50 7 RIG SERVICE 17:30 18:00 0.50 21 MAKE CONNECTION AND GO BACK TO DRILLING AFTER FIT TEST AND RIG SERVICE 18:00 18:30 0.50 2 DRILL F/ 1636 T/ 1731 18:30 19:00 0.50 7 RIG SERVICE 19:00 04:30 9.50 2 DRILL F/ 1731 T/ 2521 04:30 06:00 1.50 8 TOP DRIVE TRACK BROKE / WAITING ON WELDER

01-01-19    Drilling at 4162 -could be down and logging tomorrow Wednesday.

06:00 07:00 1.00 5 CIRCULATER WHILE WAITING ON WELDER  07:00 07:30 0.50 7 RIG SERVICE  07:30 10:00 2.50 8 FIX BROKEN PAD EYE ON TOP DRIVE FOR THE CAM AND SLIDE ON THE DERRICK  10:00 18:00 8.00 2 DRILL ACTUAL FROM 2521′ TO 3215′  18:00 01:00 7.00 2 DRILL F/ 3215 T/ 387601:00 01:30 0.50 7 RIG SERVICE  01:30 06:00 4.50 2 DRILL F/ 3876 T/ 4162

 

01-02-19    TD reached early this AM —logging early this afternoon with no additional problems.

06:00 08:00 2.00 2 DRILL ACTUAL F/4162 T/4225  08:00 08:30 0.50 7 RIG SERVICE  08:30 18:00 9.50 2 DRILL ACTUAL F/4225 T/4920  18:00 18:30 0.50 2 DRILL F/ 4920 T/ 4983  18:30 19:30 1.00 8 WELD BREAK ON BELL NIPPLE  19:30 20:00 0.50 2 DRILL F/ 4983 T/ 5204  20:00 20:30 0.50 7 RIG SERVICE  20:30 01:30 5.00 2 DRILL F/ 5204 T/5500  01:30 02:30 1.00 5 PUMP SWEEP AND CIRCULATE BOTTOMS UP / PUMP SLUG FOR WIPER TRIP  02:30 06:00 3.50 6 POOH WIPER TRIP

 

01-03-19    Reached total Depth  – Logging

06:00 10:00 4.00 6 MAKE WIPER TRIP 10:00 11:00 1.00 5 PUMP SWEEP CIRCULATE 11:00 17:30 6.50 6 POOH 17:30 18:00 0.50 8 REPAIR TOP DRIVE MANIFOLD 18:00 19:00 1.00 11 RIG UP WIRELINE FOR LOGGING 19:00 02:00 7.00 21 LOGGERS GENERATOR INOPERABLE / AWAITING BACK UP FROM KILGORE 02:00 02:30 0.50 11 M/U LOGGING TOOLS ON RIG FLOOR 02:30 06:00 3.50 11 RUN IN HOLE WITH TRIPLE COMBO / TAGGED BOTTOM 5500′ @ 0300 HRS LOGGING TOOL ON BANK AT 0530

01-03-19   Post Drill Geologic Report (see attached)

BSM Wildman #1 Post-drill Report 1-03-2019

 

RE-ENTER WELL DRILL OUT PLUGS AND PERFORATE FOR PRODUCTION

WHITEHEAD RESOURCES
BSM WILDMAN # 1
3/6/2019 Merit Oilfield working on repairing road 3/6-3/10/19
3/11/2019 Merit working on road & location, Moved in 4″ pump from Whitehead
to pump cellar, pit & levee, cut piece of 9 5/8″ casing with thread end
at Whitehead Yard and carry to location, pump cellar, found top of
cut off casing, called for welder to install threaded pup for rig, pumped
small amount of rain water from pit, started seeing solid mud at 6″ down
made decision to haul mud from pit until we estimate we have enough
pit space to drill well, pumped out ring levee around well, welder installed
pup with thread end, had 3 vacuum trucks pick up and haul out 300 bbl
mud from pit

3/12/2019 Merit finished working on road & location, road will be checked out after
rain on Wednesday to make sure it’s ready for rig move, pulled 5 loads
of mud from pit, estimated now to have enough room for drilling unless we
have problems. Merit moved in dozer to assist with rig set up, rig will
start moving in Friday 3/15/19

3/13/2019 No work on road or location today. Will check road on 3/14 after rain,
Still on go for rig move Friday 3/15, Insured well bore today for
control of well & general liability

3/14/2019 No work

3/15/2019 Moving in Sewell Drilling Rig # 2 to location, notified RRC of spud tonight
or early morning 3/16.

3/16/2019 Morning Report: Finished rigging up, started drilling top cement plug
at 2:00 am, drilled surface to 33′ fell through plug, lowered down to second
plug, tag at 370′, start drilling on same. Current drilling fluid: fresh water
Evening Report: Drilling on second plug, 530′ drilling solid cement.
Current drilling fluid: fresh water
3/17/2019 Morning Report: Current depth 1220′, drilling on third cement plug,
Current drilling fluid: fresh water
Evening Report: Current depth 1570′, drilling ahead, stopped at
1550′ to dump and clean out fresh water & cuttings from rig pit, hauled
in 300 bbl water base mud, add chemicals, displace drilled out surface
casing with mud before continuing drilling. Moved in and unloaded
5000′ of 4 1/2 casing. Current fluid in hole: 9.3# WBM
3/18/2019 Morning Report: Current depth 1812′, drilling ahead, current fluid
in hole 9.4# WBM
Evening Report: Current depth 2360′, drilling ahead, 9.4 WBM
3/19/2019 Morning Report: Current depth 2780′, making short trip, 9.4# WBM
44 vis, pump pressure 1100#, RPM- 80-90, 8-10K on bit

Evening Report: Pulled pipe to surface to inspect bit, found bit in
good shape, had heavy drag coming out of hole, checked mud,
mud weight is 9.5, vis jumped to 77 due to dehydrated mud from
old hole, had discussion about mud and mud weight, decided to
raise weight to 9.6-9.7# in an attempt to hold clay back, went back
in hole with bit, (10) drill collars, and drill pipe, had to start reaming
just below surface casing, current depth at 8:00pm- 2600′, reaming hole
3/20/2019 Morning Report: 6:00am- Current depth 3145′, mud weight 9.7#, 41 Vis,
water loss- 6, pump pressure- 1100#, RPM- 90-100, 10-12K on bit
current operations- drilling ahead
Evening Report: 6:00 pm- Current depth 3785′, drilling ahead, mud
weight- 9.7#, 41 Vis, Planning to make short trip at 4000′ before drilling
to TD.
3/21/2019 Morning Report: 6:00am- Current depth 4100′, mud weight 9.7#, 42 Vis,
5.7 water loss, 1300# pump pressure, RPM- 90-100, 10-12K on bit, made
short trip at 4000′ to check hole, no problems found with hole, currently
drilling to TD
Evening Report: 6:00 pm- Current depth 4543′, drilling ahead
3/22/2019 Morning Report: 6:00 am- Current depth 4780′, mud weight 9.7#, 42 Vis,
1350# pump pressure, RPM- 70-80, 14-16K on bit, tagged top of cement at
4657′, appear to be coming out of cement plug at current depth, current
operations- drilling ahead, moving 4 1/2″ casing onto racks and measuring
same
Evening Report: 6:00 pm- Reached TD at 4:30 pm, Total depth is 4995′
drill pipe measurements, current operations- making short trip conditioning
hole to run production casing
3/23/2019 Morning Report: 6:00 am- Laying down drill pipe, making ready to run
4 1/2″ casing
Evening Report: 6:00 pm- 4 1/2″ casing ran, currently rigging up cement
company to cement long string
12:00 Midnight- Finished cementing, rig is rigged down, mud tank is washed
out, rig is released
End of Drilling Report
 

 

 

Whitehead Resources, Ltd.
BSM Wildman # 1
Completion Progress Report
4/11/2019 Move in Cormier Well Service Rig 5, rig up, install well head
and BOP’s, schedule tubing delivery for 4/12 at 8:30 am,
Cowboy Fishing tools delivered bit, scrapper & sub, Cormier
moving in rig pump & tank

 

4/12/2019 Unload 2 3/8 tubing, measure tubing, go in hole with 3 3/4″
bit & scrapper, tag bottom at 4987′ (pipe measurements),
circulate with field salt water displacing fresh water from casing,
make ready to come out of hole for CBL on Monday morning

4/15/2019    Here on location, getting RigData up for bond log. Should have results within the next two hours.

4/15/2019 Pull tubing out of hole, remove and release rental bit & scrapper,
rig up Wrangler Wireline, run CBL & Gamma Log, cement bond
was 100%, rig down Wrangler Wireline, rig up 4 1/2″ Baker
Packer, run in hole, set packer at 4770′, test backside, install
well head, rig up Wrangler with 3′ thru tubing gun, go in hole,
perforate 4863-66′ with 60 deg phase (6 SPF), no pressure
on well, come out of hole, rig down & release Wrangler, release
Cormier Rig, ordered Swab Unit for 4/16/19

4/16/19    gas cap

4/16/2019 Move in Swab Unit, tagged fluid at 100′, pulled from 600′, second
pull fluid was at the surface, pulled from 500′, well began flowing
load water, well unloaded load water, began flowing dry gas with
1470# tubing pressure, fluid hit at around 2:00 pm, water with
trace of oil, 3:00 pm flowing 80% oil at 1380# FTP, 4:00 pm flowing
100% oil with 1360# FTP, shut well in at 5:00 pm, ordered surface
equipment.

5/1/2019  Operations manager out on location today as the well is turned to production facilities.

Pressure at tree

flare stack burning

SCREEN INSTALLATION WORKOVER

12-05-2019

Ken,

I wanted to give you an update on the progress at the Wildman # 1 well. Yesterday (12/4/19) we moved in a Cormier Well Service rig and rigged up. Today we pulled the rods, tubing & pump and sent the pump to be rebuilt (if possible). We did find sand in the bottom joints of the tubing and the plunger inside the pump barrel was stuck so there is a great possibility that we may be buying a new down-hole pump. We are currently picking up tubing and washing the hole clean to bottom. Once the hole is clean of any sand we will dump our first gravel for the screen to rest on and then we will run the screen. If all goes well we should run the screen tomorrow (12/6/19) and should finish with the workover and have the well pumping sometime on Monday (12/9/19).

Let me know of any questions you may have.

Thanks,

ANDY WHITEHEAD

12-9-2019

Photos of the screen that was run into the hole.